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notice: (The SMA stuff.)
All information contained in this article is for instructional purposes only. If you aren't sure of what you are doing when working on the suspension of your car please get help from someone that is knowledgeable in this field. In other words, if you copy what I've done here and hurt yourself, I take no responsibility for YOUR actions. |
Background CMC used a 1983 RX-7
GSL as the donor for my Locost 7. They converted
the front spindles from McPherson to double A arm suspension
by cutting the spindle tube to be ~5-1/2" long from the lower ball
joint to point where the tube was cut. A 1" long machined "cap" was
inserted and welded into
the top of the tube to allow the use of a Heim rod end as the upper
ball joint..
Apparently CMC modified various front McPherson spindles as a "one size fits all" since another CMC7 in town uses Toyota spindles and the dimensions are very similar to my RX-7 based unit. Both our front ends have extreme bump steer. Our toe in changed ~5/8" when the chassis was moved 5/8" up or down! The first generation RX-7 used a removable steering arm that also has a tapered hole for the lower ball joint shaft to be mounted to. Even if your suspension doesn't have a removable steering arm, the ideas presented in this article will still apply. The theory behind what I have done is the same for all cars. I have documented how I corrected the camber change in bounce and dive in another article, "Correcting CMC designed steering geometry, camber". These two articles are a description of all the modifications I made to correct my suspension geometry. This article is concerned with how I modified my steering arm to correct the Ackermann angle and partly bump steer. CMC suspension
design problems
My
stock CMC suspension design
had a combination of problems. These problems were caused by using the
stock RX-7
steering arms with a different track and wheelbase and the
placement of the rack & pinion. This
resulted in incorrect Ackermann affect and contributed to bad bump
steer!
The stock RX-7 steering arms are fairly long. The rack & pinion used on CMC cars has 3-1/8 turns lock to lock. The rack moves 1.48" per turn of the steering wheel. The small rack movement per turn of the steering wheel in conjunction with the long steering arms resulted in a rather large turning radius and very slow steering ratio. On a brighter note, the RX-7 1st generation spindle with its removable steering arm allows you to try various ideas to correct the steering geometry (in my case, changing of the tie rod outer end mounting point). The RX-7 steering arm is fastened to the spindle with two 14 mm diameter bolts. |
How I redesigned my suspension geometry (and things that needed to be taken into consideration) A.
Suspension design program used
I used the suspension program "Wishbone.exe" and a demo program of "Suspension_Analyzer v20_w98.exe" to redesign my suspension geometry. I basically redesigned the front suspension in Wishbone and then tweaked and finalized the design with Suspension Analyzer before the demo period ran out. Once you learn to use Wishbone it is easy to transition over to the superior Suspension Analyzer program. B.
Speed up steering ratio
C.
Steering limiter
Since the steering wheel is still able to be turned 3-1/8 turns, the mounting bolt for the new tie rod end on the steering arm can contact the lower A arm a little over 1 turn of the steering wheel in either direction. This will require that steering limiters be incorporated into the system so 2 turns lock to lock is the maximum the steering wheel can be turned. D.
Bump steer
The really bad bump steer presented a greater problem because I had to change the vertical angle of the tie rod so the extension line of the rod was correct in relation to the control arms. The extended lines of the top control arm, the lower control arm and the tie rod have to meet at a common point in virtual space with the car driving in a straight line. If I were still in the building stage I would normally raise or lower the steering rack & pinion until the bump steer was correct. My car was already built as a roller, the rack was already mounted and couldn't be raised due to other considerations. I took the "think out of the box" method of design and lowered the outer end of the tie rod mounting point instead of raising the rack & pinion. The correct angle for my car is to move the outer end of the link downwards ~1" from the original position. The tie rod now angles down towards the ground ~2° at the normal ride height. This new location is well below the original steering arm and would be located in mid air compared to where was originally located. E.
Hint
If your rack is already the correct width for your chassis and you want to speed up the steering, "just" change the mounting point of the tie rod end while keeping the instantaneous center of the rod and control arms correct. The Stalker car is a notable example of this modification. You may have to move the fore/aft mounting point of the rack & pinion at the same time. F.
Other considerations
|
In
retrospect, the
1/8" thick plate wasn't thick enough and it had a
slight amount of
flex while turning the steering wheel if the car wasn't moving. For
testing I
temporarily made 2/10" thick brackets that fit between the Heim
mounting bolt and the original RX-7 tie rod end hole to brace the
1/8" plates.
These temporary brackets stopped the flexing of the 1/8" steering arms. |
|
![]() End view of the bent new
steering arm.
You can see that the Heim bolt mounting area is bent upwards and twisted to compensate for the three angles involved. |
I've separated the
ball joint from the RX-7 steering arm. I've also started grinding the
RX-7 arm for Heim clearance and the arm support bushing (described
later).
|
![]() This shows a test fit of the
new arm in position on the RX-7 arm without the support bushing..
|
![]() End view of arm with axis of ball joint at the 12° kingpin angle and the slight upward angle of the new arm to center the Heim joint in its angular movement. |
Top view of assembled arm. The large hole had to be made big enough to clear the nut and the carter key for assembly. |
A tie rod adapter is
needed to couple each 1/2" x 20 male thread of the Heim joints to the
14 x
1.5 mm male thread of the tie rods.
This is what's left of a 1991 Nissan GS? tie rod end after I sawed the 14 x 1.5 threaded portion off of it. I centered and drilled a 29/64" diameter by 1-1/2" deep hole in the unthreaded end and threaded it for 1/2" x 20. Both threads are right hand. These were the longest 14 mm threaded rod ends I could find at the junk yard (4-1/2"). |
This is the 2" pulley that I
cut the two 1/2" thick support
bushings from.
These bushings are used to create the mounting holes on the new steering arms for the 1/2" Heims at the ends of the steering links. Each bushing will be positioned by the test steering arm and then welded to the RX-7 steering arm. |
The bushings are 1-1/16" OD x
1/2" ID x 1/2" thick. The right most piece is the remaining piece of
the pulley.
The set screw hole won't interfere with the use of the bushing. |
This picture shows the bushing
being held in the proper position just prior to welding to the
RX-7 steering arm.
|
Only the bushing itself will be
welded to the RX-7 steering arm. The set screw hole is next
to the test steering arm.
|
The bushings are now welded to
the original steering arms. I'm leaving the original steering
arm end on the arm as a place to mount the wing stays if I
decide
to mount the wings ("fenders" to us colonialists).
|
This picture shows how the Heim mounting bolt is placed in relation to the bushing and new steering arm. I am going to use the new 1/8" thick steering arm AND the bushing. I like redundancy where it counts. |
You can get a few more degrees
of Heim
angular movement if you use what are called "cones" between each side
of the Heim ball and the mounting bolt.
I have modified the bolt on the left to act as a cone. |
This view shows the lip I
machined on the
1/2" diameter grade 8 bolt to adapt it as a cone. The lip is 0.050"
high and 0.620" in diameter.
I didn't change the small chamfered surface where the head of the bolt meets the shank. |
This is the upper spacer/cone I
made from a
piece of thick 1/2" water pipe.
The length of the cone sets the vertical position of the Heim in space. It's sure nice to have a lathe. |
The next step is to
make the
steering stops. I can use spacers on the actual rack
shaft to act as limiters. The spacers will be inside the gaiters right
where the shaft emerges from the rack body. Basically I will use short tubes (or if you like the sound of it, thick washers) that will fit over the rack shaft to limit the maximum left-right movement of the rack. See the article "Rack and pinion steering limiter" for details of that modification. |
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Notice that the tie rod angle is now approximately parallel to the ground and that the extension lines from the upper & lower "A" arms and the steering tie rod now converge to the right of the picture.. The new steering arm is
sandwiched between the lower ball joint
adapter and the lower end of the spindle. It is the shiny flat area
about 1" above the lower ball joint. |
You can clearly see how much the rod end mounting point has been moved from the original location in this picture. The original mount is the open hole on the end of the RX-7 steering arm. While the tie rod still has more rearward angle than I would like, it is much better than the original RX-7 angle. |
Well for starters, bump steer affects when hitting my favorite manhole cover are gone.
Now when I bounce the front end up and down and I can see NO bump steer change with "stringing the car".
I can only move the front end a total of ~5/8" up/down by hand and at that distance the suspension program indicates that the toe change should only be 0.030". That's a GREAT improvement over the 5/8" measured toe change I had before.
Before when I entered a turn at a pretty good clip the car felt "heavy" and I had to keep a good bit of pressure on the steering wheel to maintain the turn. Now as you start the turn the car seems to turn in by itself. The pressure to maintain the turn is also lighter. As good as the car felt before, it is much better now.
The steering is definitely quicker! As a result the steering is a little heavier than before (this was expected). I ended up with the designed two turns lock to lock of the steering wheel. And I don't have to wind my arms up to turn corners anymore. A 90° street corner that used to take a 3/4 turn of the steering wheel now takes 1/2 turn.
The turning radius has decreased (also expected). Before when pulling out of my driveway and turning right onto the street, the car would end up in the far left lane of a suburban two lane street and I would then continue the turn until the car was in the right lane. Now I make the turn directly onto the right lane.
The affect of any Ackermann angle change is not as easy to detect. The main thing I noticed before was that when hand pushing the car in a tight turn that it was -very- hard for one person to move the car (this might also be an affect of the LSD rear end). It seems that the car is easier to push now (but it may just be wishful thinking). My riding lawn mower doesn't push the front end after I corrected it's Ackermann years ago.
I will check the Ackermann as soon as I find a lightly sand covered area. An old steering geometry test a real old timer taught me along with how to "feel the tires" to check toe in. Thanks Paul, wherever you are.
One of my lower ball joints is very tight (both joints are new) and I think this is the main reason why my car has no real self centering when exiting corners. With the camber and bump steer changes I can feel a very slight hint of self centering. I think once the parts wear in more that I will have some self centering affect.
All in all, I'd say the suspension changes were a great success!
Return to top of this page Other articles in this series, Go to article, "Rack and pinion steering limiter" Go to article, "Correcting CMC designed steering geometry, camber" |